Wednesday, December 17, 2014

What a productive meeting! Last week we had a staggered schedule and worked on attaching the ball lifter to the linear slides. During the team meeting portion, we discussed what progress was made since the week before and compared everyone's psuedocode. Along with this, we learned that even with the great shape and angle of the lifter design, the balls still get locked up and won't come down. This will be an interesting task, putting some kind of divider in the lifter so they will indeed fall. Other than the divider for the ball lifter, The Robot is done!

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